Keep Your Home Comfortable With Quality HVAC Services In Wallingford CT
X-Treme Temp Heating & Cooling is your go-to HVAC service provider in Wallingford, CT! We’re the experts in home comfort year-round, from AC and heating repair to ductwork and water heaters. We’ve got you covered from installation to maintenance so you can have peace of mind about your heating and air conditioning.
Read the reviews below from Wallingford, CT residents to see what your neighbors say about our expertise and customer service. We can’t wait to work with you!
Local Reviews
for Wallingford, CT
Our Reviews by City
Great Service
Stacey - Wallingford, CT 06492
Andrew was a top tier technician! Thank you!
Excellent Service Tech
Stacey - Wallingford, CT 06492
Andrew was patient, professional, and knowledgeable! Tech had to return for second day (our fault) and both experiences were great!! Andrew, thank you for a job well done! We appreciate you!
Excellent Service
Tracey - Wallingford, CT 06492
Andrew is always timely , professional knowledgeable and experienced ! He is very pleasant to speak with ! The whole staff inside and out are the best ! I would and will recommend Xtreme to anyone ! It’s extremely hard to find sincere, honest , accommodating experienced and genuine people ! Thank you all So much !
Great service
Lisa - Wallingford, CT 06492
Great service
Michael - Wallingford, CT 06492
Everything went well
Excellent service
Lia - Wallingford, CT 06492
Excellent service!
Jaime - Wallingford, CT 06492
Honest and friendly service! Would recommend to family and friends.
XTREME Brings the HEAT!
Joe - Wallingford, CT 06492
Andrew is a total professional, great guy, great tech.
Very professional and excellent service
Michael - Wallingford, CT 06492
Andrew was very efficient and professional. He solved the problem quickly and took time to explain things and field all my questions
Amazing service.
Shane - Wallingford, CT 06492
Great service. Explained everything he did and informed me of things I need to be aware of.
Excellent service
Lisa - Wallingford, CT 06492
Service was good!! Just waiting on a follow up to permanently fix my issue with the zone valve
James - Wallingford, CT 06492
Excellent service
John - Wallingford, CT 06492
Very pleased
Excellent Service!
Doll - Wallingford, CT 06492
We have had X-treme Heating and Cooling for five years. In that time they replaced our A/C and have provided service of both our heating and cooling systems. They are a family owned business that go above and beyond. They have treated us as if we are family and are honest, reliable, trustworthy and pleasant.
Response from X-Treme Temp Heating & Cooling, LLC:
We are so grateful for your 5-star review. Thanks for sharing your rating with us and the community.
As Always, Great Service!
Tracey - Wallingford, CT 06492
Excellent service!
Brian - Wallingford, CT 06492
Larry did an amazing job. Would highly recommend him and X-treme heating!
Excellent
Ken - Wallingford, CT 06492
Andrew was great and very informative
Great Service
Amy - Wallingford, CT 06492
Larry was great. So professional, clean and respectful. He explained everything to me. Wish I could request him all the time.
excellent job
joseph - Wallingford, CT 06492
Showed up on time was friendly and solved the problem quickly.
Excellent Service
Ron - Wallingford, CT 06492
Larry always gives us Great service every time. Neat, prompt, and explains everything . Very nice guy… an asset to your company. Highly recommend Xtreme. Thanks
Excellent service
molly - Wallingford, CT 06492
Great service and very professional.
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Robert - Wallingford, CT 06492
Always a pleasure to see Larry because it's understood - everything will be taken care of expertly.
Excellent service and very trustworthy
susan - Wallingford, CT 06492
Larry did a fantastic job!!!
Excellent Service
Bob - Wallingford, CT 06492
Extreme is always very responsive, courteous & not overpriced!
Response from X-Treme Temp Heating & Cooling, LLC:
We're so glad you enjoyed your experience with us. Thanks for the positive feedback.
Great service
Ken - Wallingford, CT 06492
Larry H.
When arrived, there was some oil on the floor near the oil filter canister. When the customer was trying to change the oil filter, the tank valve was not fully seated. Closed the valve and changed the filter, customer supplied. Checked the canister and found the canister was leaking on the side. Replaced the bottom half of the oil filter canister and checked for leaks. Put some odor kill on the floor near the tank.
Andrew H.
Upon arrival bled oil line of all air. Started and tested the system. Performed combustion test. 6.4%o2 80ppm co 0 smoke
Andrew H.
Brushed and vacuumed flue pipe and heat exchanger Replaced oil filter, nozzle, and strainer Checked all electrical connections and safeties Performed combustion and smoke tests 5.4%o2 45ppm co 0 smoke While performing the maintenance we found the condition of the combustion chamber had gotten worse. The sides have peeled off of the boiler wall more and back of the chamber has slightly more cracking. Recommend replacing the chamber before it collapses inwards and blocks the path of the flame. Also saw the pressure relief was dripping water. The boiler pressure was at 20 psi throughout the entire maintenance with no fluctuations indicating the expansion tank is still good. Recommend replacing the pressure relief valve. Also saw some minor corrosion starting to form on the oil line by the oil tank. Recommend replacing it in the future.
Andrew H.
Brushed and vacuumed flue pipe and heat exchanger Replaced oil filter, nozzle, and strainer Checked all electrical connections and safeties While performing the maintenance we found corrosion forming around the hot water coil on the boiler and places where the gasket is starting to get thin. Also found the combustion chamber is starting to peel off of the back wall of the boiler which will start to impact the performance of the unit. Due to the age and condition of the boiler we recommend replacing the boiler sometime in the near future. After cleaning the boiler we attempted to bleed the oil line and start the unit but found there was no oil in the oil tank. After getting customer authorization we added sludge additive to the oil tank. Need to return tomorrow to bleed the oil line, start the boiler and perform a combustion test on the boiler to ensure it is running safely. Left the boiler switch off. Travel charge to start the boiler will be $45.00 plus tax
Andrew H.
Brushed and vacuumed flue pipe and heat exchanger Replaced oil filter, nozzle, and strainer Checked all electrical connections and safeties Performed combustion and smoke tests 5.0%o2 35ppm co 0 smoke
Andrew H.
Brushed and vacuumed flue pipe and heat exchanger Replaced oil filter, nozzle, and strainer Checked all electrical connections and safeties Performed combustion and smoke tests Drained pressure from the system. Removed hot water coil plate and gasket. Scraped the face of the boiler and the plate to remove the old gasket. Installed new hot water coil gasket. Filled system back up with water and purged air from both zones. Unit is working properly. When leaving boiler pressure was 20 psi.
Andrew H.
Upon arrival unit was turned off. Customer stated the heat and the fan run continuously. Upon further investigation we found the burner primary control and igniter combo was bad internally and was still turning on even when there was no call for heat and with the tt wires disconnected. Also found 5th at the molex plug that attaches to the board was slightly loose and was causing the fan to run continuously. Removed the primary control and igniter combo. Installed a 4x4 box on the burner, mounted a new primary control, and installed an igniter. Started and tested the system. Unit is working properly now. Performed a combustion test and found when the blower turns on there is a spike in the o2 levels indicating a crack in the heat exchanger. O2 levels went from 2.1%o2 up to 2.9%o2. Took pictures and measurements for a replacement quote.
Larry H.
Performed a heating pm on a gas boiler. Brushed and vacuumed. Started and checked the safeties. Performed a combustion test. Washed the filters on the heat pumps. Checked the temps. Systems are operating properly. Filter for the main house was plugged. Washed the filters. Need to return mid season to wash the filters.
Larry H.
Performed a heating pm on an oil boiler. Brushed and vacuumed. Replaced the oil filter, nozzle and strainer. Started and checked the safeties. Performed a combustion test. 6.5% o2, 0 ppm, 85.5% efficient System is operating properly
Larry H.
Performed a heating pm on an oil boiler. Brushed and vacuumed. Replaced the oil filter, nozzle and strainer. Started and checked the safeties. Performed a combustion test. 8.2% o2, 0 ppm, 83.5% efficient System is operating properly. There was some dryer lint stuck to the prong of the transformer and on the nozzle assembly, showed the customer. The customer needs to check the dryer vent connections. There is also a hi-vent on top of the boiler that is showing some corrosion from a previous leak.
Larry H.
Performed a heating pm on an oil furnace. Brushed and vacuumed. Replaced the oil filter, nozzle and strainer. Started and checked the safeties. Performed a combustion test. System is operating properly.
Andrew H.
Upon arrival customer stated they saw a hi-vent leaking slightly the other day but it had stopped. Saw another hi-vent with very minor corrosion starting to form. After getting customer authorization we drained the pressure from the system and replaced the 2 hi-vents. When trying to fill the system up with water we found the autofeed was plugged internally and was not letting water by. Removed the old autofeed and installed a new autofeed. Filled the system back up with water and purged air out of all 3 zones. Started and tested the system. Unit is working properly. When leaving the boiler pressure was at 20 psi
Andrew H.
Cut out and removed old vent piping. Blew out the old oil line and removed it. Installed new vent piping to bring it up to code. Installed new coated oil line. Bleed air out of the new oil line. Started and tested the system.
Andrew H.
Upon arrival unit was on. Pressure was at 32 psi and the pressure relief was dripping. Drained some pressure from the boiler with the autofeed valved off and the pressure immediately went back up to over 30 indicating the expansion tank had gone bad. After getting customer authorization we drained pressure from the system and removed the old expansion tank and pressure relief valve. Installed new expansion tank and pressure relief valve. Filled the system back up with water and bled all zones of air. Started and tested the system. Unit is working properly. When leaving boiler pressure was at 20 psi Need to return at some point to replace the autofeed. After replacing the expansion tank and pressure relief we brought the pressure up to 15 psi but the autofeed continued to add water even when the system didn’t need it.
Andrew H.
Brushed and vacuumed burner tubes Inspected and vacuumed burner, blower compartments and surrounding area Checked electrical connections and safeties Checked gas pressure Performed combustion test Inlet pressure-5.722 in.w.c. Manifold pressure- 2.991 in.w.c. 9.7%o2 27 ppm co Replaced16x25x1 air filter
Andrew H.
Brushed and vacuumed flue pipe and heat exchanger Replaced oil filter, nozzle, and strainer Checked all electrical connections and safeties Performed combustion and smoke tests 5.1%o2 30 ppm co 0 smoke Recommend having a chimney person come out and clean the chimney. Soot is starting to back up in the chimney and starting to block the flue pipe entrance Greg’s chimney 203 630 1976 Wallingford plumbing 203 269 6175
Larry H.
Performed a heating pm on an oil boiler. Brushed and vacuumed. Replaced the oil filter, nozzle and strainer. Started and checked the safeties. Performed a combustion test. 5.5% o2, 0 ppm, 84.8% efficient System is operating properly.
Larry H.
Performed a heating pm on an oil boiler. Brushed and vacuumed. Replaced the oil filter, nozzle and strainer. Started and checked the safeties. Performed a combustion test. System is operating properly.
Andrew H.
Performed a heating pm on an oil boiler. Brushed and vacuumed. Replaced the oil filter, nozzle and strainer. Started and checked the safeties. Performed a combustion test. 3.1% o2, 0 ppm, 87.2% efficient System is operating properly. There was air in oil line when starting it up. The line goes overhead. The fuel pump is starting to get stressed. Recommend installing a tiger loop. 3 systems- total 739.14
Andrew H.
Upon arrival unit was on and running. Customer stated the upstairs zone was not receiving heat. Checked all zone valves and found the zone valve for the upstairs zone was receiving power but was not opening. Replaced the zone valve and tested the heat on that zone. The heat in that zone is working now but we found there was some air in the lines. The autofeed is not letting enough pressure through to bleed the zones of air. Recommend replacing the autofeed so we can remove the air from the heating loops. Also recommend replacing the hi-vent on the boiler and the circulator gaskets due to corrosion.
Larry H.
Turned the system on and it started to rumble. Found the system very dirty. Replaced the oil filter at the tank which was plugged. Blew out the oil line. Replaced the strainer and nozzle. Brushed and vacuumed the boiler. Started and tested. Performed a combustion test. System is operating properly. The back flow preventer is leaking slowly. Recommend replacing. Recommend adding a sludge additive to the tank to help clean the oil.
Andrew H.
Oil furnace pm Brushed and vacuumed flue pipe and heat exchanger Replaced oil filter, nozzle, and strainer Checked all electrical connections and safeties Performed combustion and smoke tests 4.7%o2 40 ppm co 0 smoke
Larry H.
Customer reset the control prior to arriving. Customer turned the thermostat on and the burner started. Checked the oil flow, the was some air in the line. After shutting off on reset and the bleeder open, the oil line went into a vacuum. Found the oil filter very dirty and restrictive. Blew out the oil line, there was no resistance in the line. Replaced the oil filter and bled the line. The system runs properly and there is no air in the line.
Andrew H.
Upon arrival water heater was off on reset. Pushed the reset button and it lit right away. Heckled oil flow and had poor flow with a lot of air in the line while the furnace was running. Checked the oil flow with the furnace off and had ok flow but still had some air. Checked the strainer and it was clean. Checked the oil filter and found it was starting to get dirty and could be restricting the oil flow to the water heater. Changed the oil filter and bled the oil line. Started and tested the system. Unit is working properly.
Andrew H.
Upon arrival unit was on but not running. Had customer turn the heat up and the furnace started with no issue. Checked oil flow and had good flow. Checked the nozzle and found it was covered in oil and had carbon buildup starting to form on the nozzle assembly. Checked the igniter and found it was starting to slightly turn yellow/orange which indicates the igniter is starting to get weak. This would cause a delay in ignition and cause a loud noise. Replaced the igniter and started and tested the system. Unit is working properly.