Keep Your Home Comfortable With Quality HVAC Services In Wallingford CT
X-Treme Temp Heating & Cooling is your go-to HVAC service provider in Wallingford, CT! We’re the experts in home comfort year-round, from AC and heating repair to ductwork and water heaters. We’ve got you covered from installation to maintenance so you can have peace of mind about your heating and air conditioning.
Read the reviews below from Wallingford, CT residents to see what your neighbors say about our expertise and customer service. We can’t wait to work with you!
Local Reviews
for Wallingford, CT
Our Reviews by City
Excellent service!
Kirsten - Wallingford, CT 06492
Larry was very nice. He was even kind to my dogs. Thank you.
Excellent service, highly recommend!
susan - Wallingford, CT 06492
Andrew was here to clean our furnace today, and as always did a fantastic job. He found a few minor things that needed replacing and showed me the parts. Also, after 30 years of boiling hot water, he said our mixing valve needed replacing, must of asked a dozen plumbers and furnace people over the years with no results. These people are the real deal, so happy we have them!
Excellent service, thank you Larry!
Joan - Wallingford, CT 06492
I highly recommend Extreme Temp heating and cooling. Great service, reliable and reasonable, and responsive.
Great service
Eric - Wallingford, CT 06492
Fantastic!
Katharine - Wallingford, CT 06492
Amazing service! Courteous, on time and knowledgeable!
Prompt and efficient
LJ - Wallingford, CT 06492
Any time XtremeTemo comes they are efficient and the quality of their work is top notch.
Excellent service
Mary - Wallingford, CT 06492
Excellent Service
Zack - Wallingford, CT 06492
Excellent service
Annamarie - Wallingford, CT 06492
Andrew was knowledgeable, professional. Very pleased.
Owner
John - Wallingford, CT 06492
Larry was great fixed the issue with my AC in no time definitely will call again.
Service call
Karen - Wallingford, CT 06492
Great job
Rick - Wallingford, CT 06492
always a great job! they have my complete confidence and trust
Excellent Service
michelle - Wallingford, CT 06492
He was very thorough worker
Excellent service and personable
Janet - Wallingford, CT 06492
Excellent
Mary - Wallingford, CT 06492
Satisfied Customer.
luke - Wallingford, CT 06492
Andrew did a great Job! He seemed to have a great attention to detail, and kept me in the loop every step of the way.
Excellent and timely service!
Susan - Wallingford, CT 06492
Andrew is so helpful and takes the time to explain everything to me. He addresses my concerns and leaves everything so neat and running smoothly.
Excellent service
Brian - Wallingford, CT 06492
Larry has been out to our home on other occasions and is always courteous and respectful. He is knowledgeable and explains things in a manner that could be understood. The service he provides is excellent.
Excellent customer service
Sue - Wallingford, CT 06492
Larry came and fixed our central air on one of the hottest days of the year. He squeezed us in, now that is great customer service!!!
Professional Service
joe - Wallingford, CT 06492
Very professional, and detail oriented.
Excellent Service!!
Mark - Wallingford, CT 06492
Same day service! Explained the problem and fixed it in less than 30 minutes
Great service!
Shanielle - Wallingford, CT 06492
We couldn’t be more happy with the quality of work we received. The technician was extremely knowledgeable and was very honest about what he saw and gave suggestions long the way. You can tell that he genuinely cares about his job and wasn’t looking to “add more work” to charge more money. I fully trust the work done! Thank you for everything!
Great job
Donald - Wallingford, CT 06492
Great job
Prompt tesponse
Nick - Wallingford, CT 06492
Great service. Fast response always calls back quickly
Excellent Service!
Lagase - Wallingford, CT 06492
The technician was amazing. Very thorough and easy to understand when he was explaining what needed to be done e.

Andrew H.
Brushed and vacuumed flue pipe and heat exchanger Replaced oil filter, nozzle, and strainer Checked all electrical connections and safeties Performed combustion and smoke tests 7.8%o2 0 ppm co 0 smoke

Larry H.
Performed a heating pm on an oil boiler. Brushed and vacuumed. Replaced the oil filter, nozzle and strainer. Started and checked the safeties. Performed a combustion test. 6.1% o2, 25 ppm, 83.3% efficient System is operating properly.

Larry H.
Performed a heating pm on an oil furnace. Brushed and vacuumed. Replaced the oil filter, nozzle and strainer. Replaced the air filter, 16x25x1 Started and checked the safeties. Performed a combustion test. 7.9% o2, 33 ppm, 86.5% efficient System is operating properly. Performed an A/C pm. Blew out the drain line. Rinsed the condenser. Checked the electrical connections, checked the pressures and temps. System is operating properly. The capacitor is rated for 45/5 +/- 5% mfd, the actual was 44/1.4 mfd. The fan side is below the limits. Also the fan motor is drawing the max rated amps of 1.2 amps. The fan motor is very loud. Recommend replacing the condenser fan motor and capacitor. - the customer is turning off the system and wants to replace everything in the spring. The water heater is from 2015, recommend replacing. Customer has scheduled an appointment to replace the 40 gallon Electric hot water heater w/ a Taco Leak Breaker and pan.

Andrew H.
Brushed and vacuumed flue pipe and heat exchanger Replaced oil filter, nozzle, and strainer Checked all electrical connections and safeties Performed combustion and smoke tests 9%o2 2ppm. O 0 smoke While performing the maintenance we found the firomatic oil valve handle was starting to go bad. The solder ring was starting to fall to the bottom of the handle. Attempted to thread on a new handle but found the stem of the oil valve was spinning freely. After getting customer authorization we replaced the oil shut off valve. Customer stated the hot water is very hot. Tested water temps coming out of the water coil and the mixing valve. The water temp coming out the mixing valve was only 2-5* colder than coming out of the water coil indicating the mix g valve is letting too much hot water through. Recommend replacing the mixing valve and moving it further away from the water coil. Manufacturers recommend having it at least 10 inches away due to high temps. 1/2 mixing valve

Larry H.
Performed a heating pm on an oil furnace. Brushed and vacuumed. Replaced the oil filter and nozzle. Checked the air filter. Customer recently replaced it. Started and checked the safeties. Performed a combustion test. System is operating properly. The furnace is older and the oil line goes into the floor at the tank and coms up by the furnace. Recommend replacing the line.

Andrew H.
Performed oil pm on boiler and ac pm Brushed and vacuumed flue pipe and heat exchanger Replaced oil filter, nozzle, and strainer Checked all electrical connections and safeties Performed combustion and smoke tests 8.8%o2 8ppm co 0 smoke Visually inspected indoor evap coil and blower compartment Checked all electrical connections and safeties Checked volts and amps Visually inspected air filter Rinsed condenser coil Blew out drain line and poured water to ensure properly draining Tested condensate pump Checked refrigerant levels Checked capacitor Took temps While performing the ac maintenance we found the condenser coil had a high buildup. Was able to get the buildup off with water but recommend rinsing the condenser in the future.

Andrew H.
Brushed and vacuumed flue pipe and heat exchanger Replaced oil filter, nozzle, and strainer Checked all electrical connections and safeties Performed combustion and smoke tests 7.8%o2 3ppm co 0 smoke While performing the maintenance we found the porcelain on the nozzle assembly was broken and missing a very large section. After getting customer authorization we replaced the porcelains with new ones. Started and tested the system.

Larry H.
Isolated and drained the domestic water coil. Removed and installed a new Caleffi Mixing Valve. Adjusted the mixed water temp to 127-135*F.

Andrew H.
Brushed and vacuumed flue pipe and heat exchanger Replaced oil filter, nozzle, and strainer Checked all electrical connections and safeties Performed combustion and smoke tests 9%o2 18ppm co 0 smoke Upon arrival when watching the furnace start up we noticed the burner motor sounded worse than last year and is getting close to failing. After getting customer authorization we replaced the burner motor. Started and tested the new motor. Unit is working properly. Replaced air filters

Andrew H.
Brushed and vacuumed flue pipe and heat exchanger Replaced oil filter, nozzle, and strainer Checked all electrical connections and safeties Performed combustion and smoke tests 7.0%o2 0ppm co 0 smoke

Andrew H.
Valved off old water heater. Drained old water heater of water. Cut out and removed old water heater. Installed new 50 gallon electric water heater with nearby piping. Installed Taco leak breaker on the cold water line. Filled water heater up and purged air from the water heater. Started and tested the water heater.

Andrew H.
Performed oil pm on oil furnace Brushed and vacuumed flue pipe and heat exchanger Replaced oil filter, nozzle, and strainer Checked all electrical connections and safeties Performed combustion and smoke tests 4.7%o2 12ppm co 0 smoke While performing the maintenance we found very high levels of sludge on the oil filter. Recommend getting sludge additive for the oil tank. Also found a flue pipe 90 for the water heater is starting to rot and fall apart. Taped the section for now but recommend replacing the 90 before the corrosion gets worse. Flue pipe repair is $50.00 6 inch flue pipe Greg’s chimney 203 630 1976 Sept 15th 9 am

Larry H.
When arrived, the blower at the furnace was running. Checked the system and found the Fan Switch on the thermostat was turned on. Turned the switch off and the blower turned off. Set it to cool, the blower turns on but the condenser did not start. The contactor was pulled in and there was 247 volts at the unit. Checked the capacitor, found both sides of the capacitor are bad. The capacitor is the component that starts the compressor and the fan motor. The capacitor needs to be replaced. Replaced the capacitor, started and tested. System is operating properly, 56*F discharge air.

Larry H.
Removed old combustion chamber, gasket, and debris. Installed a new combustion chamber and gasket. Started the boiler and let it run for 25 minutes for the chamber and adhesive to cure. Perform combustion and smoke tests. Pressure relief: Drain pressure from the system. Remove old pressure relief and install new pressure relief. Fill system back up with water. Purge air from all zones. Start and test system for proper operation.

Andrew H.
Brushed and vacuumed flue pipe and heat exchanger Replaced oil filter, nozzle, and strainer Checked all electrical connections and safeties Performed combustion and smoke tests 5.5%o2 4ppm 0 smoke

Andrew H.
Brushed and vacuumed flue pipe and heat exchanger Replaced oil filter, nozzle, and strainer Checked all electrical connections and safeties Performed combustion and smoke tests 6.9%o2 0 ppm co 0 smoke While performing the maintenance we found the oil line is starting to corrode. Since the oil line is in the concrete the lime in the concrete is starting to oxidize the copper. Would recommend replacing the oil line in the near future. Also found the water heater is from 2014. Would recommend replacing that in the near future as well. Typically recommend replacing water heaters every 10 years. Had to cut the metal on the furnace where the oil line enters since we could not remove the strainer housing. Made the hole larger and now the strainer can be easily removed. Oil line is roughly 20 feet

Andrew H.
Brushed and vacuumed flue pipe and heat exchanger Replaced oil filter, nozzle, and strainer Checked all electrical connections and safeties Performed combustion and smoke tests 6.8%o2 3ppm co 0 smoke

Andrew H.
Performed 2 oil pms Brushed and vacuumed flue pipe and heat exchanger Replaced oil filter, nozzle, and strainer Checked all electrical connections and safeties Performed combustion and smoke tests Furnace- 7.5%o2 40 ppm co 0 smoke Water heater- 7.1%o2 3ppm co 0 smoke While performing the maintenance we found very high levels of sludge in both oil filter canisters. Would recommend getting sludge additive for the oil tank

Larry H.
Checked the RTU, the unit was off on system lock out. Reset the unit, the blower started then the compressor. The condenser fan motor started but was moving very slow. The fan motor is bad and needs to be replaced. Picked up new Fan motor and installed. Replaced the capacitor. Started and tested. Checked the pressures. System is operating properly.

Andrew H.
Opened boiler door and removed old combustion chamber. Cleaned and vacuumed soot and any debris from the old chamber. Installed new combustion chamber and gaskets. Close burner door and start the boiler. Ran the boiler for 20 minutes continuously to let the new chamber and gaskets cure. Performed combustion and smoke tests. 8.2%o2 7ppm co 0 smoke Burner motor may need to be replaced in the future.

Larry H.
Recovered the refrigerant back into the condenser. Removed and and installed a new warranty Evaporator Coil at the furnace. Pressure tested and evacuated the system. Opened the valves and released the refrigerant back into the system. Started and tested. Adjusted the charge to 13* subcooling. System is operating properly.

Larry H.
Performed a heating pm on an oil boiler. Brushed and vacuumed. Replaced the oil filter, nozzle and strainer. Started and checked the safeties. Performed a combustion test. 4.9% o2, 41 ppm, 86.3% efficient System is operating properly. Performed an A/C pm. Blew out the drain, checked the air filter, customer replaced it. Checked and tested the condensate pump. Rinsed the condenser. Checked the electrical connections, checked the pressures and temps. 11* subcooling , 54* supply, 70* return System is operating properly.

Andrew H.
Performed 2 a/c pms Visually inspected indoor evap coil and blower compartment Checked all electrical connections and safeties Checked volts and amps Visually inspected air filter Rinsed condenser coil Blew out drain line and poured water to ensure properly draining Tested condensate pump Checked refrigerant levels Checked capacitor Took temps When performing the maintenance on the second floor system we found the unit was slightly low on refrigerant. After getting customer authorization we added 1 lb 410A to the upstairs unit While performing the maintenance for the main floor unit we found the capacitor was open internally and had gone bad. After getting customer authorization we replaced the 35/5 capacitor. Started the unit and found it was low on refrigerant. After getting customer authorization we adde 4.5 lb R410a to the downstairs unit. Also added UV dye to both systems. Units are working properly. Need to call and schedule leak search

Andrew H.
Recovered the refrigerant from the old system. Removed old air handler, condenser, line set, thermostat wire and electrical whip. Installed a Trane XR14, 2 1/2 ton condenser and a Trane TEM6 variable speed air handler in the attic. Installed new condenser pad, line set, thermostat wire, and electrical whip. Brazed in all new refrigerant connections. Pressure tested and evacuated the system. Started the system and added addition refrigerant as needed. Had 79* return air and 61* supply air.

Andrew H.
Upon arrival unit was off on reset. Went to check for oil flow when we found the firomatic handle’s lead ring had failed and dropped causing the oil shut off valve to close. Removed the old firomatic handle and replaced it with a new one. Checked for oil flow and had good and clean flow. Checked the nozzle and had no dripping in the blast tube. Checked the past run history from the primary control and found the system was running great until the handle failed. Started and tested the system. Unit was running at 4.7%o2 3pp co 0 smoke with 160 ohms. Unit is working great.